Tapstone Energy Reports Two Mississippian Producers In Dewey County, Okla.
Drilling Activity Details
OK
United States
Drilling Activity Summary
Description
In Dewey County, Okla., Tapstone Energy LLC completed two Anadarko Basin-Mississippian producers. The #1H Sportsman 3-18-16, Section 3-18n-16w, is flowing 6.16 MMcf of gas, 364 bbl of 49-degree-gravity condensate and 1.09 Mbbl of water per day from an open-hole zone at 10,635-15,766 ft. Following acidizing and fracturing, it was tested on a 44/64-in. choke with a shut-in tubing pressure of 2,780 psi and a flowing tubing pressure of 1,108 psi. It was drilled to 15,766 ft and the true vertical depth is 11,064 ft. The Oklahoma City-based company also completed #1H Seifried Trust 4-18-16 in Section 4-18n-16w. Production is from a fracture-stimulated and acidized north lateral at 10,660-15,894 ft in Mississippi Solid. It initially flowed 7.5 MMcf of gas, 230 bbl of 54-degree-gravity condensate and 1.704 Mbbl of water per day. The 16,003-ft well has a true vertical depth of 11,436 ft and it was tested on a 38/64-in. choke with a flowing tubing pressure of 1,700 psi and a calculated absolute open flow rate of 24.8 MMcf of gas per day.
In Dewey County, Okla., Tapstone Energy LLC completed two Anadarko Basin-Mississippian producers. The #1H Sportsman 3-18-16, Section 3-18n-16w, is flowing 6.16 MMcf of gas, 364 bbl of 49-degree-gravity condensate and 1.09 Mbbl of water per day from an open-hole zone at 10,635-15,766 ft. Following acidizing and fracturing, it was tested on a 44/64-in. choke with a shut-in tubing pressure of 2,780 psi and a flowing tubing pressure of 1,108 psi. It was drilled to 15,766 ft and the true vertical depth is 11,064 ft. The Oklahoma City-based company also completed #1H Seifried Trust 4-18-16 in Section 4-18n-16w. Production is from a fracture-stimulated and acidized north lateral at 10,660-15,894 ft in Mississippi Solid. It initially flowed 7.5 MMcf of gas, 230 bbl of 54-degree-gravity condensate and 1.704 Mbbl of water per day. The 16,003-ft well has a true vertical depth of 11,436 ft and it was tested on a 38/64-in. choke with a flowing tubing pressure of 1,700 psi and a calculated absolute open flow rate of 24.8 MMcf of gas per day.