Woodford Completion Produces 14.2 MMcf Of Gas, 91 bbl Of Condensate Per Day
Drilling Activity Details
Grady
OK
United States
Drilling Activity Summary
Description
In Grady County, Okla., a Woodford discovery was tested flowing 14.2 MMcf of gas, 91 bbl of 56-degree-gravity condensate and 4.463 Mbbl of water per day. Denver-based Camino Natural Resources LLC’s #1WH Michael 0607 11-2 is in Section 13-6n-7w. Production at the Watonga-Chickasha Trend well is from fracture-stimulated perforations at 16,588-22,968 ft. It was drilled to the west to 23,028 ft, 15,797 ft true vertical, was 5,303 psi and the flowing tubing pressure was 928 psi. and bottomed in Section 2-6n-7w. Gauged on a 30/64-in. choke, the shut-in tubing pressure was 5,303 psi and the flowing tubing pressure was 928 psi.
In Grady County, Okla., a Woodford discovery was tested flowing 14.2 MMcf of gas, 91 bbl of 56-degree-gravity condensate and 4.463 Mbbl of water per day. Denver-based Camino Natural Resources LLC’s #1WH Michael 0607 11-2 is in Section 13-6n-7w. Production at the Watonga-Chickasha Trend well is from fracture-stimulated perforations at 16,588-22,968 ft. It was drilled to the west to 23,028 ft, 15,797 ft true vertical, was 5,303 psi and the flowing tubing pressure was 928 psi. and bottomed in Section 2-6n-7w. Gauged on a 30/64-in. choke, the shut-in tubing pressure was 5,303 psi and the flowing tubing pressure was 928 psi.