Marathon Announces Results From Three Meramec In Watonga-Chickasha Trend
Drilling Activity Details
Blaine
OK
United States
Drilling Activity Summary
Description
Three Blaine County, Okla., Mississippian completions were announced by Marathon Oil Corp. The Watonga-Chickasha Trend wells were drilled from a pad in Section 23-15n-11w. The #3-23-26MXH Chapman 1511 was drilled to 19,291 ft, 11,431 ft true vertical, and produced 1.802 Mbbl of oil, 6.36 MMcf of gas and 2.392 Mbbl of water per day. It was tested on an 18/64-in. choke and production is from perforations at 11,429-19,170 ft. The #4-23-26MXH Chapman 1511 was drilled to 19,578 ft, 11,858 ft true vertical, and produced 764 bbl of oil, 3.331 MMcf of gas and 3.413 Mbbl of water per day. It was tested on an 18/64-in. choke, and production is from perforations at 11,720-19,364 ft. The #5-23-26MXH Chapman 1511 was drilled to 19,370 ft, 11,643 ft true vertical, and produced 1.867 Mbbl of oil, 6.955 MMcf of gas and 2.17 Mbbl of water per day. It was tested on a 20/64-in. choke and production is from perforations at 11,642-19,173 ft.
Three Blaine County, Okla., Mississippian completions were announced by Marathon Oil Corp. The Watonga-Chickasha Trend wells were drilled from a pad in Section 23-15n-11w. The #3-23-26MXH Chapman 1511 was drilled to 19,291 ft, 11,431 ft true vertical, and produced 1.802 Mbbl of oil, 6.36 MMcf of gas and 2.392 Mbbl of water per day. It was tested on an 18/64-in. choke and production is from perforations at 11,429-19,170 ft. The #4-23-26MXH Chapman 1511 was drilled to 19,578 ft, 11,858 ft true vertical, and produced 764 bbl of oil, 3.331 MMcf of gas and 3.413 Mbbl of water per day. It was tested on an 18/64-in. choke, and production is from perforations at 11,720-19,364 ft. The #5-23-26MXH Chapman 1511 was drilled to 19,370 ft, 11,643 ft true vertical, and produced 1.867 Mbbl of oil, 6.955 MMcf of gas and 2.17 Mbbl of water per day. It was tested on a 20/64-in. choke and production is from perforations at 11,642-19,173 ft.